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Glenn's
Supercharged Bluebird Wagon
I
have been playing around with these Datsun motors for years. Although I
also own a 350 Monaro, I just love the little datsuns.
The
beauty of the Datsun is parts interchangeably. Using the right combination
of standard datsun parts can build a potent little motor.
The
motor is a L18.
Crankshaft
is a double counterweight version. I avoid using the single weight cranks.
The
flywheel is off a L24 six cylinder motor, much lighter than the standard
unit and accepts the larger diameter clutch plate and pressure plate, which
is off a 720 four wheel drive. Gearbox is the standard 5 speed. Oil pump
is modified by drilling a 1/4 inch hole near the 3/8 hole at the top of
the pump, where it mates with the timing cover, I'll have to take a photo
to explain this, but it increases oil pressure at low RPM, important for
a blown motor due to the extra torque below 2000rpm.
I use
L16 conrods as they are 2.9mm longer than the L18 rods. This improves the
rod ratio from 1.66 to 1.7, giving more bottom end torque. The standard
datsun piston has a 2.9mm deep dish in the top. So by fitting L16 conrods
and machining the piston flat, you end up with a zero deck height, flat
top piston bottom end, than has a better rod ratio than the L20B (1.68).
Pistons are 60 thou oversize, however I have taken these motors to 140
thou over and used toyota pistons. They must have a thick bore.
The
head is a A87. Inlet ports are simply ported to L20B head size ports. Exhaust
ports are heaverly modified and now flow 80% of the inlet port. The standard
datsun has a very poor exhaust port compared to its inlet port. The problem
with the exhaust port is the gentle taper from small to large port area
just after the port turns behind the valve. Trick here is to make the exhaust
port shorter! But I'll keep this little trick to myself. Port flow improves
heaps and as a bonus you get anti-reversion. The combustion chamber is
reshaped around the spark plug and smoothed.
I
kept with the standard valves, but cleaned them up. As the cam is a standard
unit I used standard valve springs, no sense in wasting power pushing heavy
springs down when it doesn't need them and the motor wont be revved above
6000. The rockers are ground flat where they are wiped by the cam. By flattening
and polishing this wipe pad, the valves are opened and closed quicker,
without changing duration or lift. In effect a slightly larger cam. Its
an old Ford 2L trick.
I originally
had a couple of 2inch SU carbies off a Rover fitted to the motor to run
it in. This little motor ended up VERY torquey, I was surprised and pleased.
The
supercharger was purchased from Adelaide Jap Weckers, give these guys a
plug
for me will you, they were very helpful. The supercharger is from a Toyota
GZ motor (I think). It is a roots type with a built in sump with its own
dip stick, teflon rotors and an electric clutch, and uses a multi-V type
belt drive.
To
drive the blower I found a waterpump pulley from a late model Corolla,
and with a bit of machining fitted it to the front of the crank shaft.
This drives the blower via a serpentine belt and idler pulley. A DCOE 42
carbie is mounted on the blower with a home made adapter plate and linkages.
Outlet of the blower is fed into a standard L20B inlet manifold with another
home made adapter.
Mounting
the blower proved to be a pain. The car is air conditioned and up here
in Mackay you need it, so I had to mount the blower above the air-con compressor.
With a supercharged motor you need to make the distance from carby to motor
as short as possible. You cant use a blow through setup like a turbo motor
as a blower will stall the motor when the throttle is closed, or bend the
throttle plates, or pop a hose, whatever, it will break something!! That
boost pressure has to go somewhere and you will need a bloody great popoff
valve to get rid of all that air! A turbo will simply stall or slow down,
but the blower is driven by the crankshaft.
To
get the blower as close as possible to the motor I had to move the dizzy.
I looked into a angle drive, then a toothed belt drive, ended up using
a direct drive off the front of the cam shaft. I had a lump of aluminum
welded on the front of the tappet cover, then with the help of Ross Torrisi
of Torrissi's Garage, made a boring bar that uses the Datsun cam towers
to center itself. We bored a hole in the tappet cover to suit a sigma dizzy.
The tappet cover was also doweled to the head so it would align perfectly.
I had to use a sigma dizzy as the cam shaft spins in the opposite direction
to the normal dizzy drive, so a datsun dizzy would retard as rev's increased,
where the sigma unit is designed to spin the other way.
The
dizzy was shortened, then a 19mm socket fitted to the drive shaft. Once
installed,
this socket fits over the cam sprocket bolt and drives the dizzy. I removed
the guts of the dizzy and machined a new breaker plate to take a standard
datsun twin point assembly. The points are angled 10 degrees apart, and
the second set of points is used when the boost pressure reaches 3 pounds
as sensed with a pressure switch (out of a washing machine!! $2 from the
local junk yard and is even adjustable), effectively retarding the timing
by 10 degrees. The points switch a Ford ign module and coil.
Exhaust
manifold is standard, flowing into a 2 inch system.
The
setup works like this -
Normal
driving, blower off.
The
blower free spins due the the air passing through it, this gives a very
slight lag in the throttle response. Car drives ok, economy is good.
Blower
on.
A
switch on the gear stick (I was thinking of Mad Max when I fitted it) engages
the blower. Response is instant, no turbo lag here! Total boost pressure
is 5 pounds at full throttle, even as low as 1500 RPM !!!! Boost pressure
remains constant through rev range. Motor is VERY bloody torquey and doesn't
ping at all, even with 9.5:1 compression, fuel economy is bloody terrible!
I haven't
raced the car at out local drag strip yet, but from past experience I feel
the car would do a low 15, high 14 second pass, but the top end speed would
be high as it goes very hard in the top gears.
One
problem is the carbie behaves differently when blower is on. Running this
setup is like bolting a carbie onto a 2L motor, tuning it, and then expecting
it to run on a 3L motor, just doesn't work. One solution would be to remove
the clutch setup on the blower, and mount a smaller pulley. This way the
blower is on all the time and it will be easier to tune the carb, plus
giving more boost.
Latest
news -
I now
wish to sell the complete blower setup, as I need the funds to get me
old
Monaro back on the road.
For
$1000 you get
-Blower
-Adapter
plates and manifolds
-Crank
pulley and idler
-Pressure
switch
-Boost
Gauge
-Air
cleaner but no carbie, I need it for another project.
-Modified
tappet cover and dizzy
Glenn
Littleford glenn@orion-online.com.au
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